Service Manual For Mf Gc2310
Massey Ferguson GC2310 2005 - 2008 Backhoe loader tractor Next model:. Production: Distributor: Massey Ferguson Manufacturer: Iseki: Iseki 1.1L 3-cyl diesel Capacity: Fuel: 5.5 gal 20.8 L: Rear Type: I Rear lift (at ends): 1,190 lbs 539 kg: Rear PTO: independent Rear RPM: 540 Mid PTO: optional independent Mid RPM: 2000: Wheelbase: 57.1 inches 145 cm Weight: 2,600 lbs 1179 kg: Dig depth: 78 inches 198 cm Dump angle: 43 inches 109 cm GC2310 Serial Numbers: - Serial numbers unknown.
Massey Ferguson GC2310 TLB Repair How To Repair 2006 Massey Ferguson GC2310 Tractor Loader Backhoe. Introduction This web page contains a narrative log and pictorial essay to maintain a 900 hour with a 22.5 hp 3-cylinder Iseki L3 1.1L (69 in 3) diesel engine. This page is meant to document technical data, and motivate and encourage you as you try to fix your tractor. I have other pages about my 230,000 mile. And 100,000 mile, and 160,000 mile. I appreciate your link back to this page so Google thinks what I say is important. Because the Model GC2310 comes standard with a backhoe and front loader instead of 3-point hitch, you'll also hear it called 'TLB' for 'Tractor Loader Backhoe'.
The PTO, 3-point lifters, and tow-ball mount plate are all there, just covered by the backhoe. Mine also has two hydraulic loops installed after market - the rear loop is controlled by a baby joystick to the left of the seat and the front loop is controlled by a click button switch on the bucket joystick.
Lastly, mine came with an operator cab to keep the operator more comfortable if operating in cold / wet conditions. March 2016 - Buying Manuals T he first problem I worked after purchasing the tractor wasn't really a problem. I just wanted owner, parts, and maintenance books. AGCO (who purchased an owns the Massey Ferguson line) has an (login as guest to view books), so there's really no reason to buy the paper parts manual. I ordered 4 paper books, which immediately highlighted the fact that there is a serial number break in the GC2310 series.
Massey Ferguson Gc2310 Manual
They refer to it as 'N 25201', which means any tractor with that serial number or after has a different parts catalog and a different operating manual. To interpet that serial number, you have to add the common letters. 'JNA 25201' is what you would find on your tractor. The tractor serial number is behind your left heel; don't confuse that with the frame serial number or engine serial number. My serial number is JRAxxxx, and because R comes after N, I have the later model. An easy way to tell the difference is that the newer serial numbers have a tachometer around the hour-meter.
Here are the paper book part numbers for a GC2310 with a serial number JNA25201 or later. Check the AGCO parts web info if you want ot confirm - be sure to choose the English lanuage if that is what you want. If you order from AGCO, you can get DVD versions for a few dollars cheaper with noticeably less shipping cost. In order to work on the front axle, you need the wheels off the ground. You can use the bucket to lift up the front of the tractor and then put a jack stand under the frame near the front axle.
Use a 19mm socket to remove the wheel studs and remove the wheel. To open up the final gear housing, I worked a chisel around and around the silicon seal. If you look carefully there are notches on the left and right side in order to catch a screwdriver blade and pry open the seal. Also remove the outer tie-rod taper bolt so the final wheel housing can come totally off the tractor. Look in the housing just above the small gear.
You can see the snap ring that must be strentched open and removed from its notch. My snap ring pliers spread the ring barely far enough. The final gear housing will drop away from the shaft. You could replace the seal without removing the 90 degree gear housing. It depends on the seal sleeve installed on the upper part of the shaft. If it's really stuck or rusted into position, you'll want to be able to work around all sides of it and that is way easier if the 90 gear housing is not connected to the tractor.
Remove the 90 degree housing if you want. The rubber seal is a 2-piece thing. You have to remove one piece from inside the lower piece.
You have to remove the collar from the outside of the upper piece. Mine were very tightly installed and I needed to use a chisel to break the metal part of the oil seal before pushing / sliding / twisting them to remove them. After removed, clean everything up with solvent and confirm you haven't damaged the shaft or bearing housing. Putting the new seal in place involves lubricating it and pushing, pressing, or gently tapping it them into position. Re-lubricate the seal and put the gear housing back up onto the spindle. Hold it in position while re-installing the snap ring. To reconnect the final gear cover, I scraped off all the old silicone rubber, filed off one little blemish, and touched up the entire surface with emery cloth.
I cleaned everything with gasoline and then rinsed the surface with acetone to remove any oily residue. I applied silicone rubber as a gasket and re-assembled it.
I measured the bolts as 9 mm in diameter. The service manual identifies torques for only 8 mm or 10 mm bolts.
I used the high end of 8 mm as my target and torqued everything to 20 ft lbs. If you pulled off the 90 degree gear housing, there is no way to get a torque wrench on the bolt heads.
I used a 1' long open end box wrench and pulled the wrench with a 20' fish scale in order to get 20 ft lb of torque. I put hydraulic fluid into the right gear housing through the top bolt hole in case there was an air bubble trap somewhere, and then added more in the left axle fill cap up to a half-filled axle. Side note - after about a day of work, I noticed the left spindle was starting to seep oil out. I think I need to go replace the other seal, too.
I think the right leak was keeping the fluid level low enough to not affect the left side, but with the right side fixed, the fluid level stays high enough to make the left leak visible. I will have to order another seal and repeat in the near future. May 2016 - Replace Steering Rod Ends The right steering rod end had no rubber boot on the inner ball joint and the ball and joint were totally rusted and very loose.
The left one was badly cracked and the inner ball joint was rusty and loose. I wondered if I could operate the tractor this way until one of the ball joints just popped out. For a car, this would be bad because the toe-in would wander around and it would probably make bad rattling noises when on the road and would probably wear out the front tires really quickly. However, a tractor is bouncing around on uneven loose surface most of its life so I'm not sure the tires would ever know the difference. Eventually, I decided to buy new ball joints so as to not let little maintenance items build up. Turns out you can't buy just the inner ball joint any more. That part has been superceded by another part, which has been superceded by another part.
The final part (7069209M91, $73) is an aggregate kit that includes everything outboard of steering rod out to the tie rod tapered bolt. It does not include the big flat washer where the rod end screws into the hydraulic piston and it does not include a lock washer or castle nut for the tapered bolt. Spoiler alert: the cotter pins and 10mm-1.25 castle bolts on the tapered bolt were very rusty. I ended up having to get new of both.
The hardware store sold a package of 100+ miscellaneous cotter pins that notably did not have the one size I needed (3/32' diameter an inch or longer), so I drove back and bought the package of the exact size. The castle bolt was made out of a normal grade (hardness) nut by cutting slots with a cutoff wheel grinder. I will have to watch these and see if the nuts are too soft, or loosen. When removing the tie rod, if the taper bolt is stuck tight, consider using an air chisel. Don't hit any tractor part with an air chisel. Back the bolt off until it's flush with the end of the bolt.
Then use a thick aluminum bar or plate between the nut and bolt and the air chisel. The softer aluminum takes the hammer blows and transfers the impacts to loosen the bolt without damaging the bolt or nut. This method has reliably removed tie rod end bolts in every vehicle I've tried it with.
The tie rod ends screw into the ends of the hydraulic actuating rod, separated with a large flat washer that prevents the tie rod from crushing in against the oil seal when the steering wheel is turned hard left or right. In order to screw / unscrew these connections you have to be able to grab the rod ends and the rods with a wrench and turn about 20 ft lbs. The flat sections provided to do this are very narrow, so I had to grind down my tools to make them fit. Two 'special' tools are required. A narrow 19 mm open end box wrench for the flats on the stainless steel hydraulic drive rod. A wrench of this size was not economically available alone, so I picked up an entire set of metric wrenches for $9 from Harbor Freight. I'm not sure their tools are hard or accurate enough for regular commercial use, but for an open end box wrench that will get ground down and used once every 3 years, I appreciated the lower price.
A narrow 28 mm open end box wrench for flats on the tie rod ends. I could not find a 28 mm wrench for sale other than in a $50 kits, so I used a 10' crescent wrench, which opened jaws just enough to fit. I picked up a $6 version from Harbor Freight because I had to grind down the width of the jaws to fit onto the narrow flats of the tie rod ends, and didn't want to grind on my main shop tools. Because there was no rubber left on the old rod ends, I could use a fat-jaw pipe wrench to take them apart. Turning in opposite directions, one would let loose first. Luckily the left one came off first, exposing the flats on the end of the stainless rod.
I did not have to grind down the thickness of my 19 mm wrench. To unscrew the right tie rod, I used a pipe wrench while holding the stainless rod on the other end with the 19 mm wrench. To re-install the tie rod ends into the stainless steel rod, I couldn't use a pipe wrench because it would have crushed the rubber seal. Instead, I used the narrow-jaw cresent wrench to fit over the tie rod ends without interfering with the big flat washer. I put the right rod end on first using the stock 19 mm wrench.
To install the left one, I had to use the narrow 19 mm open end box wrench to not interfere with the big flat washer. I pushed what felt like about 20 pounds on the end of my approximately 1 foot long wrenchs. I put the taper bolt castle nut back on to 20 flt lbs with a torque wrench and then backed off only enough to slip a cotter pin through the first available nut slot.
I preset toe-in by counting tie rod end thread grooves on the old rod ends. Mine had 3-1/2 threads exposed on each side. After putting the tires back on the tracter, I checked alignment for the spec'd 2-6 mm of toe in (front of tires closer together than the rear of the tires).
Nothing fancy, just a tape measure held against the tire surface at mid-axle height measured between two 2x4 sections held against the outside of the tires (someone helped me on the other side of the tractor). I found about 1 mm of toe in with weight off the front wheels. I will check and adjust again after the hardware has settled for a week or so. Summer 2017 - Removed the biggest stump The prior year, I cut down a big leaning tree. I did use the backhoe to try digging out some of the stump, but didn't get very far. All winter and spring the stump stayed in the backyard and had a moat around it whenever it rained.
I knew I'd have to get it out, eventally. The tractor in the picture is 4' wide.
The stump is slightly wider and taller. It was a BIG stump.
At first I was coming at the stump head on with the backhoe and digging from several positions around the stump. I just couldn't get the depth required. I ended up modifying my technique by digging deep 4' trenches on the left and right side of the stump instead of in front of it.
I did this from 4 positions around the stump. Very soon I had a pillar of dirt in a deep hole. When I stood in it, I was up to my chest in dirt. I tried pulling the stump and dirt pillar over using a full-size van, but the rear wheel just spun in the grass. I hooked up a chain to the tractor in 4WD and tugged and relaxed over and over - maybe 20 times and finally the pillar of dirt tipped over, but t here was no way I could pull or lift or drag it out of the hole.
If I released tension, it immediately tipped back. I used a log about 8' in diameter to block the stump, as shown in the picture.
I put a little dirt under the stump and then removed teh log. Tthen I pulled the stump over the other way pulling from the other side, and added a few shovels of dirt under the stump on that side.
After about 15 back and forth pulls, taking several hours, I slowly put more and more dirt under the stump until it was all the way out of the hole-or more accurately, the hole had been slowly filled in under the stump. I tried pushing or lifting it and that was a total no-go. The stump is not moving. We'll burn spare sticks and brush under the stump for several months - maybe even into next year. But eventually it will be gone.
What's interesting is that the very heavy clay dirt is cooked by the fire and turned into firebrick. Every once in a while I go chip some off and do another fire. May 2018 - Left Front Steering oil seal I need anotehr steering shaft seal (4265156M91). I'll order from McFarlane Mfg, Saulk City, WI.
JacksSmallEngines.com said they don't sell Massey parts any more). Waiting for parts.
Massey Ferguson Gc2310 For Sale
June 2018 - Hydraulic Hose As I backed the tractor into parking, I noticed a steady drip of hydraulic fluid coming from the front left side. Turns out the cylinder end of the 'bucket down' line on the left side was oozing fluid out between the hose and the crimp of the connector. Time to replace the short flexible section of hose. The AGCO parts diagram on line shows it as a 1/4' hose 13' long, part number 71515711. I unscrewed the 1/4 I.D. Hydraulic line from the cylinder side and found a male SAE O-ring Boss (a.k.a.
ORB) fitting with threads that measure 0.555' across. This is the type with the O-ring around the collar, not 'flat face' where the O-ring is on the face end of the threaded part. On the other end, the hose disconnected from the metal tubing, revealing a JIC female connector on the hose with 0.509' I.D. On the female thread.
The JIC male threads on the metal tubing measured 0.559' O.D. Across the threads.
Marking a pen-line on a piece of paper and a protractor confirmed the 37 deg angle of a JIC connector (not a 45 deg JIC or 30 deg Japanese JIS). Now I needed to match my measurements against the industry standard options. Checking a, I found. JIC SAE-6 size male threads are 0.5625' O.D., with the closest alternative 0.50' and 0.75'. JIC female SAE-6 threads are 0.53125' I.D.
With the closest alternative 0.46' or 0.60'. Since I measured 0.559' and 0.509', my guess is they are SAE-6 with 9/16-18 threads. ORB-6 size male threads are the same as SAE-6 and I measured 0.555'.
Choices are 9/16' (0.5625') or the metric connector that looks almost identical which is M14x1.5, or 0.5512'. Since the one end is SAE JIC, I'm betting the other end is not metric. I have 'SAE-6' and 'JIC-6' size connectors. The hose is a 3000 PSI hose with an outside dimension of 0.50' and a length of 13.25' (end of metal connector to end of metal connecto).
I think it's 1/4' SAE 100R17 single-wire hose with a 2' minimum bend radius. Alternately, fatter O.D. 1/4' SAE 100R16 hose might work, with an O.D. Of 0.57' and a bend radius of 2' and working pressure of 5800 psi. The 100R16 doesn't seem to be much fatter, but when it's squeezed into various body channels of the tractor, the size does matter.
On the backhoe, I expect the narrower 100R17 is required to get all the hoses packed in next to each other. I called around to price a replacement. Advanced Auto Parts doesn't make hydraulic lines. Jack's Small Engine again shows that they do carry Massey Ferguson parts.
$31.25 after shipping. O'Reilly Auto Parts referred me to a sister store in a nearby city and they priced it out at $34.73 before tax. I priced out the assembly at discounthydraulichose.com and it came out to $29.37 after shipping.
I checked SurplusCenter.com and they only have stock hose lengths, but the 12' was close. Turns out I could buy a 12' 100R17 hose with 1/4' NPT fittings each end , and a 1/4' NPT female - ORB male adapter and a 1/4' NPT female - JIC female connector. It probably would add up to about 13-1/4'. Total price after shipping came out to $20.45.
One of the adapters had a 4-month backorder delay. Instead of the 4 month back order, at SurplusCenter, I found the 0.070' fatter 100R16 2-wire hose with different end connectors: female JIC-6 connectors. Then all I needed was a single male JIC to male ORB adapter. I accepted the fater 100R16 hose. Total price was $18.40 shipped. I found torque specifications for hydraulic lines and put the adapter on the end of those.
I connected the ORB end to the tractor first because the entire hose has to rotate while tightening the connector; 24-26 ft lb. On the JIC side (connected to the cylinder), the nut allows me to tighten the connection while holding the hose untwisted; 17-19 ft lbs. Everything checked out fine.
The only caution issue is that with an adapter on the end adding up to the specified 13' length, the non-bendable end of the hose is longer. That doesn't matter for a mostly straight run installation. For a 'U' shaped installation like the loader-up hose, this probably wouldn't matter, either In this case, however, the loader-down 'S' shaped installation makes the 'S' stretch more than I like because the flexible rubber part of the 13' is shorter. In reality, the hose I removed was really 13-1/2' anyhow. Testing the loader full up and full down looks like it will work - it just pulls harder sideways than I would like at the full loader-up position.
Two months later, the loader-up end of the same cylinder started oozing fluid right through cracks in the hose. I should have purchased two! Also, the 'un-curl' hose on the backhoe bucket is starting to ooze fluid at the top bend of the arm.
I need another 13' hose and a 128' hose. Both have ORB at the cylinder end. The loader-up needs JIC like the one I just did. The backhoe bucket looks like it terminates with ORB at the operator control block, too. What to do with your tractor Here are a few projects I've used the tractor for.
Dig and pull tree stumps and level yard dirt. Now, each normal sized stump removal is about 1 hour (with tractor and axe) instead of 1 day with a shovel and axe. Backhoe out bamboo weed patch and scoop out tangly weeds with the bucket. Build a 6' privacy mound of dirt. Lift and move rail road ties and 10' sections of tree trunks.
Bucket and backhoe have chain hooks welded on which have been very helpful. Front bucket about 6' high is a platform for me to stand on to reach tree trim branches - be sure nobody moves the bucket control while standing on the bucket!.
Safety pull on tall trees and large branches as I cut them down (so the tree falls the correct direction). I learned that the tractor can pull pretty hard and it just cracked off one 8' diameter branch that was 1/2 cut through. I am careful to cut bark all around now so it won't tear back if the branch snaps off early. Removed raised dirt gardens from against the house. Nip and lift rail road ties out of position. Without teeth on the bucket, I can't dig with it very well, so I backhoe all the dirt first and then the bucket scoops the loose dirt easily.
With a hooked chain, 2 or 3 wraps around rebar lets the front bucket pull the rebar out of the ground. Carry cut firewood and drop it into a pile for splitting. Of note, not only is the transport much easier but I don't UNload the logs now - I just dump them. Redistribute the slope of the yard where water used to collect. Use the backhoe to strip 2' thick sections of grass and replant the grass in new locations. Dig out a drainage ditch across the front of the property, and free debris from around the culverts.
Moving dirt for therapy after a rough day at work, trying to make a tall mound. Teaching skills to my friends and family. Dig bricks and stones out of old paved patio area and leveled dirt for concrete. Dig off 2' of dirt to make way for a stone walk-way. Carry tools in the bucket to a job site so I can make only one trip. Backhoe out difficult honey suckle roots and clear area to smooth and level by back scraping with the bucket. Air chisel old bricks and concrete in the bucket and then all the chips and dust can be easily dumped to level my driveway without scooping/shoveling up the shards.
Dig out around 4x4 concrete anchors and then use a chain on the bucket to pull the old concrete and wood out of the ground. Please contact me using the copyright link prior to commercial use, or reproducing for distribution in a commercial context.